Refining Community Logo

Effects Of Iron Sulfide Contamination & Filtration In A  Liquid Treating System

By Nicholas Brownrigg, Howard Energy Partners & Orbie Harris IV, Transcend Solutions, LLC,

Introduction 

Produced condensate and other unprocessed hydrocarbon liquids of varying gravity often hold  substantially less marketing value than processed and stabilized condensate, due to the large range of components in the liquid, its volatility towards vapor flashing, and contaminants either due to  the composition of the liquid or chemicals used in its production or transport. For this reason, there  are many facilities, whether integrated into larger plants or stand-alone, that serve the purpose of  processing these raw, off-spec liquids into higher valued products, such as 9 psi RVP (Reid vapor  pressure) stabilized condensate or Y-grade NGL. 

9 psi RVP condensate is often used in blending with crude oil and fuels and is free from light end  hydrocarbon components prone to flashing, thus making it a very stable hydrocarbon liquid  product. Because of its stability, it can be transported to a sales point without the need for  pressurized tanker trucks. RVP is a measure of the volatility in the liquid and is determined by the  ASTM-D-323 test method. 

Y-grade NGL typically consists of lighter end hydrocarbons and is transported by pressurized  pipeline to fractionation sites where it is separated into its constituent components (typically  ethane, propane, i-butane, n-butane, and heavier fractions) for marketing to users who have a need  for these purity products. Because Y-grade consists of more volatile, lighter end hydrocarbons, it is necessary to keep them pressurized to ensure that no vapor flashing occurs during transport.  Specifications for Y-grade are usually set by the pipeline owners that transport these liquids,  though most pipeline operators’ specifications adhere to highly similar metrics. 

Y-grade NGL must meet specifications for the amount of sulfur species that are present in the Y grade. These include a test for hydrogen sulfide (H2S) present in the Y-grade, the amount of total  sulfur species in the Y-grade, as well as the corrosiveness of the Y-grade (typically influenced by  sulfur, and primarily H2S, in the Y-grade). To reduce the amount of H2S present in Y-grade NGL,  an amine treating process is usually employed, which involves the contact of the Y-grade NGL  with a mixture of amine and water, causing the H2S in the Y-grade to be absorbed by the amine,  such that the effluent Y-grade passes the aforementioned tests. 

Howard Energy Partners (HEP) owns and operates a facility in South Texas principally responsible  for the collection and processing of off-spec condensate and other hydrocarbon liquids to a 9 psi  RVP product and a Y-grade product that employs an amine treatment process for the Y-grade  product before custody transfer to a pipeline.

While the amine treatment process for the removal of CO2 or H2S is widespread throughout several  industries, there are still many operational issues that can arise from the process. The amine  treatment process requires a strict adherence to maintaining a delicate chemistry and purity balance to properly work as intended. A change in composition or concentration in the amine or feed stream  being treated can easily upset the process, causing severe operational issues, and inadequate amine  treatment.  

HEP recently encountered such an issue with amine chemistry and filtration at its Live Oak facility.  A discussion of the issue and its resolution is contained herein. 

Facility Background 

Howard Energy Partners’ (HEP) Live Oak facility is located in Three Rivers, TX in the Eagle Ford  Shale play, and was one of first facilities built by Howard Energy Partners after its incorporation.  Live Oak is an off-spec condensate receiving and processing facility which receives many truckloads of liquids from different sources throughout South Texas each day. Live Oak is capable  of processing off-spec condensate of a vast and varying composition, and because of this, receives  trucks from area refineries and other field production sites simultaneously, which may contain  different levels of H2S or chemical contamination (methanol, for example). 

The Live Oak facility’s processing set up consists of a truck unloading area that allows trucks to  offload into several large off-spec condensate bullet vessels. These vessels hold multiple  truckloads of off-spec condensate product received and, as previously stated, often contain liquids  of varying blended composition. When filled, these Off-Spec Condensate Tanks are pumped to a  Stabilizer system that contains a Stripper (pre-frac) Tower and a final Stabilization Tower. The Stripper Tower produces an off-gas product that is compressed and then dehydrated and sent to a  downstream pipeline. The Stabilization Tower produces a 9 psi RVP stabilized condensate product  off the bottom of its reboiler and Y-grade NGL product from the reflux of the tower. The 9 psi RVP  stabilized condensate is stored in atmospheric storage tanks, and the Y-grade NGL is pumped to a  downstream pipeline. 

Because H2S is typically present in the loads received at the Live Oak facility, the Y-grade product  often sees an unacceptable amount of H2S out of the Stabilization Tower as it pertains to meeting  pipeline-grade product specification. For this reason, an NGL Amine Treater is installed  downstream of the Stabilization Tower for the Y-grade product before it is sent to pipeline. The  NGL Amine Treater consists of an NGL Amine Contactor Tower, and an amine regeneration  system for the effluent rich amine. In the NGL Amine Contactor, the Y-grade product is passed  through an amine column, where the amine absorbs any H2S or CO2 present. Once treated, the Y grade is considered on-spec and can be sent to pipeline using the downstream pipeline pumps. 

The rich amine exiting the bottom of the NGL Amine Contactor is sent to the Amine Regeneration  system to remove the absorbed H2S and CO2 components, so it can be reused downstream in the  amine contactor for further absorption. The rich amine is flashed down to a lower pressure to free 

any entrained light hydrocarbons, which are recovered as fuel gas within the process. The amine  is then passed through a series of filters to remove any remaining entrained hydrocarbons, debris,  or solid particulates (which will ultimately be the discussion of this paper). After filtration, the rich  amine is sent to a still tower where CO2 and H2S components are boiled off in a reboiler at high  temperature. This acid gas stream is scrubbed in a Sulfaguard unit (H2S scavenger system) to  remove H2S before being flared/vented, and lean amine leaves the reboiler before being cooled  and recycled to the amine contactor tower. For the purposes of this paper, it is important to note  that the equipment in the amine system predominantly consists of carbon steel material of  construction on all major vessels and piping. 

Figure 1 – Simple Block Flow Diagram for Live Oak Facility 

The Live Oak Facility is designed to process a capacity of 10,000 bpd of inlet condensate from the  off-spec condensate storage and produces a varying amount of 9 psi RVP product and NGL  depending on inlet condensate composition. The amine system is designed to handle 7000 bpd of  NGL and has a design amine flow rate of 20 gpm. 

Y-Grade Product Spec Issues Appear 

Upon its commissioning, the Live Oak facility operated with no, or sparing, need for the amine  treating portion of the facility, as the liquid loads delivered to the facility via truck were  contaminant-free enough to produce a product meeting pipeline specifications by just stabilizing  the trucked in liquids. As there appeared more commercial need and benefit to accepting truck  loads with higher concentrations of contaminants, the amine treating unit was placed into  operation. The amine treating unit operated as designed and without issue for several years.

Late in 2018, HEP operations team at Live Oak began noting that the Y-grade product leaving the  amine treating portion of the plant to pipeline had started to fail the copper strip corrosion test which is required for Y-grade pipeline specifications.  

The copper strip corrosion test is an ASTM standard test used to qualitatively measure for the  presence of sulfur species in the Y-grade; if the copper strip inserted into the Y-grade is tarnished,  it indicates that there are sulfur species in high enough concentration within the Y-grade such that  it does not meet pipeline specification, while no-to-minimal tarnishing indicates a pass of the test. 

Y-grade is within specification if it meets 1A or 1B standards, per the ASTM copper strip corrosion  standard chart in Figure 2. 

Figure 2 – ASTM Copper Strip Corrosion Standards 

The intermittent inability to pass the copper strip corrosion test in the Y-grade product leaving the  Amine Treater led to the Live Oak facility facing the possibility of being shut-in from its Y-grade  product pipeline, which would lead to lost revenue due to lost processing time and create a liquids  bottleneck for the upstream producers who feed the facility. 

With the cause of the copper strip corrosion failure unknown at the time, switching to a different  grade of amine was explored with the hopes of resolving the issue. The Live Oak amine treater  had originally been designed and operated using a DEA-based amine. A switch to Dow CR-402 amine was eventually proposed to treat for unaccounted mercaptan species, which at the time was  the hypothesis for why the copper strip corrosion test was failing. To reuse some of the DEA in the  system, UCARSOL CR-402 was used as makeup amine until such a time that the system only  contained UCARSOL CR-402. 

The amine system ran mostly without issue for several years after the amine changeout, continually  meeting Y-grade product specification until late December 2022. At this time, the copper strip  corrosion test failures began to resurface, and the operations team had indicated several operational issues with the unit, particularly in the Amine Still. The Amine Still tower was noted to be showing  severe temperature swings on the overhead, ranging anywhere between 140°F to 215°F, rapidly  losing temperature at times and not remaining at the desired setpoint of 215°F despite constant  heat input via the reboiler, indicative of amine foaming issues. 

In December of 2022, Dow’s technical service team was again engaged for support in diagnosing  the issue causing the copper strip corrosion failure. It was recommended to drain the water from  the Reflux Drum on the overhead of the Amine Still tower and make up with fresh water to the  system. The system did see improvements from this, as each time the Reflux Drum was drained,  the copper strip test would pass and the operational issues in the Amine Still would subside.  However, these gains in performance would be fleeting, and the issues would appear again around  5-7 days after draining of the Reflux Drum. The Reflux Drum was drained, and the water replaced  multiple times with the same result before attempting another solution.  

During the process of draining the Reflux Drum on a constant basis, the inlet feed trucks to the  Live Oak facility were measured using Draeger tubes for sulfur species concentration to attempt  to determine if there was a certain feedstock to the facility that was large enough in sulfur content  in the feed condensate from the off-spec vessels that could cause the product Y-grade to ultimately  fail a copper strip test. The findings led to the conclusion that while there were multiple loads into  the Live Oak facility that did contain sulfur species other than H2S, they were not in high enough  concentration to generate issues in the Y-grade after blending out with other truck loads without  mercaptans/other sulfur species.  

When the copper strip failures and operational issues in the Amine Regeneration system reemerged  in late 2022, operations also noted that the Amine Contactor and Amine Still sight glasses were  filled with a black debris, that the Pre-Carbon Filter on the Amine Regeneration skid was full of  foam and several of the previously spent filtration cartridges contained black debris. Additionally,  amine samples appeared to have a very dark hue, both in samples collected from the lean side and  rich side of the Amine Regeneration system. 

Figure 3 – Amine Foaming in Pre-Carbon Filter, Black Debris on Filter Cartridges, and Amine Samples

While the source was still unknown, the buildup of the black solid debris in the Amine Contactor  and Amine Still was a cause for concern, and it was determined that the Live Oak facility would  take a brief shutdown to open the Amine Still and clean out the black debris present in the vessel.  After cleaning the Amine Still of the black debris, the facility consistently passed the copper strip  corrosion test and saw no operational issues again for approximately one month. Once the copper  strip corrosion test failures and operational issues returned, it was noted by operations staff that  the Amine Still again was filled with black debris. 

Figure 4 – Solid Black Debris Recovered from Amine Regeneration System 

The presence of the black debris throughout the Live Oak facility’s Amine Treater system and its  reappearance after being cleaned out led to the HEP’s discovery of literature (referenced in the  References section at the end of this paper) that discussed the fouling of Amine Systems. The  papers discussed a black build up in amine units treating H2S commonly referred to as “shoe  polish”. The description of this “shoe polish” material was similar to what HEP was seeing in the  Live Oak Amine Treater. While “shoe polish” tends to have a more gummy consistency (indicating  the presence of other contaminants that give it this consistency), the effects of “shoe polish”  mentioned in the paper and the coloring matched what was being seen in the Live Oak Treater. 

From the literature, it was determined that this “shoe polish” material forms due to iron sulfide  particles that are created during the reaction of the amine with H2S in the liquid NGL being treated.  In the reaction of the amine with the H2S in the liquid NGL, sulfur ions can also react with iron  ions present in the steel used in the piping and vessels of the Amine System to form iron sulfide  solid particulates. In many systems, these iron sulfide particles form on the sides of the vessels and  piping in the amine system and form a protective layer against corrosion due to sulfur within the  unit. However, if velocities of fluid moving through the vessels/piping is high enough, the iron  sulfide particles can be washed away, or not allowed to settle, and can circulate throughout the  system, contaminating amine and leaving the steel prone to potential sulfur corrosion. 

Knowing that iron sulfide is constantly produced during the reaction of the amine with the NGL  liquid helped to put into perspective why the black debris reformed in the Amine Still after its  cleaning. Additionally, from the literature, iron sulfide particles in a high enough concentration in  an amine system is known to cause severe foaming in amine and lead to amine process upsets,  similar to what was being observed in the Live Oak Amine Treating system, particularly in the  Pre-Carbon Filter during changeouts as noted in Figure 3. 

With this knowledge, the HEP operational team began to formulate the hypothesis that the high  concentration of what was presumably iron sulfide in the amine was either causing one or both of: 

a.) Foaming in the Amine Still leading to improper regeneration of the amine, and a failure to  properly treat for H2S in the Amine Contactor, leading to a failed copper strip corrosion  test. 

b.) Foaming in the Amine Contactor leading to carryover of rich amine into the downstream  treated NGL. The downstream NGL filter, which is designed to remove trace amounts of  amine, was being overwhelmed with amine volumes exceeding design, leading to a failed  copper strip corrosion test, due to high concentrations of rich amine in the NGL post-filtration. 

Because the Stabilizer and Amine Treating units were operating at their design capacities and not  exceeding these limits, it was determined that the velocity in the unit could not necessarily be  reduced to slow the process generating the iron sulfide without limiting the throughput to the  facility. Therefore, the filtration on the rich amine side of the Amine Regeneration system would 

need to be examined for continuously generated iron sulfide particle removal. Additionally, with  the existing amine within the system having heavy quantities of iron sulfide dissolved into it, the  amine would need to be substantially filtered to avoid requiring another costly amine changeout.  

Transcend Solutions was engaged to test the solids loading in various locations in the process. The  Amine Still, Amine Contactor, and Amine Regenerator were tested to determine the elemental  composition of the particulate in the system, and to also determine the efficiency of the existing  filtration system. 

Evaluation of Solid Particles, Amine, and Existing Filter Performance 

Once at site, Transcend Solutions collected samples of the solid black debris from the Amine  System at the Live Oak facility, as well as several of the spent Pre-Carbon Filter elements. The  solids and elements collected underwent a variety of tests at Transcend’s lab to determine their  composition. The results of these tests are described below:  

– A solvency test was performed on the solid black particulate. Xylene and heptane were  used to determine the total amount, if any, of hydrocarbons present in the sample. Much of  the sample remained undissolved indicating that it was inorganic in nature.

– A magnetic separation test was performed on the dried solids using a strong magnetic  source. It was determined that the solids were ferrous in nature, due to their affinity for the  magnetic source. 

– Scanning Electron Microscopy (SEM) was performed on the filter elements collected from  the Live Oak site, and the particle size was determined to range between 2 microns to  greater than 10 microns. See Figure 5. 

– Energy Dispersive X-Ray Spectroscopy (EDS) was performed on the filter elements  collected from the Live Oak site. Analysis showed S and F with an atomic percent of 66.3  33.7%, respectively, indicating a form of ferrous sulfide was present in the system. See  Figure 6. 

Figure 5 – SEM Particulate Sizing

Figure 6 – EDS Spectroscopy with Atomic Percentage Per Element 

These results indicated that the black debris recovered was likely to be metal sulfide particles.  

Transcend Solutions also performed online gravimetric analysis on the Pre-Carbon Filter and Post Carbon Filter in the Amine Regeneration system at points upstream and downstream of the filters.  This test determined the particulate concentration in samples of the amine upstream and  downstream of each of these filters. See Table 1. The online gravimetric analysis has been  described previously as critical to accurately determine total suspended solids (TSS) analysis of  samples which are at risk of solid formation on contact with air – which are liquid samples with  high levels of dissolved iron (such as amine and sour water samples). Online gravimetric analysis  is used to determine particulate content in a variety of fluids. This method is particularly  advantageous when it is desired to capture the particles directly from a process fluid while in  operation, minimizing the risk that derives from artifacts caused by reaction of the fluid with air  exposure. 

Unit / Vessel Inlet (mg/L)Outlet (mg/L) Removal
Pre-Carbon Amine / F-305 0.6 0.5 17%
After-Carbon Solids Filter/ F-307 3.5 5.8 0%

Table 1 – Gravimetric Analysis Results

Based on the results of the gravimetric analysis of the two filter units, it was determined that the  Pre-Carbon Filter showed a 17% removal of the particulate in the amine, while the Post-Carbon  Filter showed a 0% removal of the particulate in the amine. Typical removal at this stage should  be 95% or greater. 

Based on this gravimetric analysis, it was determined that a minimal amount of the solid  contamination present in the amine was being removed by the existing filtration, and that the solids  would continue to build up within the amine system, causing operational issues unless an  alternative solution was deployed. The 17% solids removal efficiency observed in the Pre-Carbon  Filter was inadequate to maintain proper operations of the Amine Treater, and indicative of both undersized filtration and inadequate removal efficiency for the service. 

Iron Sulfide Removal Solution 

HEP relied on Transcend Solutions to provide a filtration solution that could remove the buildup of iron sulfide particulates in the amine system at the Live Oak facility, that would then resolve  the unit’s operational issues and stop the copper strip test failures. 

Transcend Solutions proposed a two-step solution for HEP’s amine unit. The first step was to  utilize a filtration vessel from Transcend’s rental fleet to help remediate the iron sulfide problem  in the near term. The second step was to design a fit-for-purpose filtration unit that could handle  the particulate load present in the system, while minimizing the amount of work required from the  HEP operations team for filter changes. A process overview, showing where samples for testing  were collected, and rental vessel tie-in locations can be seen in Figure 7. 

Figure 7 – Live Oak Filtration Flow Diagram with Sample Locations and Rental Vessel Tie-In Points 

The rental filter provided by Transcend Solutions to operate in lieu of the existing Pre-Carbon  Filter is shown in Figure 8. The rental filter was approximately 200 gallons in volume with thirty-

six (36) 10-micron Tetra Endur coreless filter elements, utilizing high efficiency Novacel™ media. The rental unit was significantly larger than what would be custom-designed for the permanent filter solution, which would be installed at a later time. 

Figure 8 – Installed Rental Vessel at HEP Live Oak Facility 

With the rental vessel online, the amine stream began to clean up and allow the Live Oak facility  to return to 1A/1B copper strip test results. In approximately 3 weeks, the Live Oak facility was  able to return to full process capacity. 

Unit / Vessel Inlet (mg/L)Outlet (mg/L) Removal
Rental Vessel Sample 1 10.7 0.5 95%
Rental Vessel Sample 2 10.7 0.4 96%

Transcend Solutions then provided a custom-designed permanent filter for the Amine Treater at  Live Oak to replace the existing Carbon Pre-Filter and rental filter previously used. This filter was  designed to minimize piping and skid rework at the Live Oak site, which in turn helped keep  installation costs low. Additionally, the size and number of elements in the filter was optimized to  give the operations staff at the Live Oak facility ample time between changeouts. While final  installation of the permanent filter was not complete at the time of the writing of this paper, the  permanent filter is designed to achieve a removal efficiency of 99.98% on all particulates greater  than 10 microns in the amine stream. This filter will be installed on the Live Oak amine  regeneration system once fabricated to provide ample iron sulfide removal from the amine stream. 

Conclusions 

It is important in amine treating systems to maintain the proper chemistry between the feed stream  being treated and the amine in the system to ensure proper treatment in the unit. Any deviation in  contaminant concentration in the feed stream or amine stream, or a drop in concentration of the  amine stream, among other variables, can upset the treatment process. 

The treatment of H2S with amine in carbon steel vessels leads to the production of iron sulfide  particulates that can become entrained in the amine stream, and lead to significant foaming in the  amine, which jeopardizes the amine’s ability to be properly regenerated in conventional amine  regeneration systems. Additionally, foaming amine can be carried over out of the amine contactor  tower to the downstream system, risking potential recontamination of treated fluid.  

Ideally in amine systems treating for H2S, iron sulfide particles would be handled by designing the  unit such that velocities remain low enough that the iron sulfide passivates the walls of the  equipment and piping, forming a protective layer to corrosion between the treatment process and  the steel constituting the equipment. Because the velocities in the Live Oak system’s design were  not conducive to this, a filter designed to the correct size and media specification to remove iron  sulfide from the amine stream was necessary to install in the process. 

Once iron sulfide particulates were adequately removed from the amine stream in the Live Oak  Amine Treater, the foaming witnessed in the amine subsided, and subsequently so did the unit’s  operational issues and downstream Y-grade specification failures. 

Further studies are still underway to understand whether the cause of the foaming and associated  operational issues and specification failures were due to an inability to regenerate the amine  properly in the Amine Still or due to amine carryover into the product Y-grade out of the Amine  Contactor.  

However, regardless of mechanism, the root cause of the issues experienced at the Live Oak  facility was due to iron sulfide production within the Amine Treating unit, and its inability to be  removed due to inadequate and undersized filtration. Adequate vessel sizing and filtration design  are both essential for effectively removing particulates from the amine stream and maintaining  fluid quality. With adequate element design, effective filtration in some cases may be achieved  with undersized vessels, but in the case of the Live Oak facility, an undersized vessel and  improperly designed filtration elements both contributed to the process failure. Even if the 

vessel was sized correctly for the system, the current element design in use would not have  achieved the desired amine quality and would have required an upgraded element that was  appropriate for the fluid and particulate challenge. 

References 

1. Scanlan, Thomas J. and 3M Purification Inc, “Filter Media Selection in Amine Gas  Sweetening Systems”, Laurance Reid Gas Conditioning Conference, Norman, OK,  February 23-26, 2014. 

2. Beke, Louis, “Contamination in Amine Systems”, BSDT Seminars, September 2010.

Leave a Reply

Your email address will not be published. Required fields are marked *

Posted by: The Refining Community

Refining Community